Electric Power ›› 2015, Vol. 48 ›› Issue (4): 16-22.DOI: 10.11930/j.issn.10.11930.2015.4.16

• Column of Flue Gas Denilralion • Previous Articles     Next Articles

Evaluation on Effects of SCR Ammonia Injection System Modification for Flue Gas Denitrification

WANG Lele1, ZHOU Jian1, YAO Yougong2, YAO Yan1, SONG Yubao1, FANG Chaojun1, CHEN Weiwu2   

  1. 1. Xi’an Thermal Power Research Institute Co., Ltd., Suzhou Branch, Suzhou 215011, China;
    2. Huaneng Haimen Power Plant, Shantou 515132, China
  • Received:2015-01-22 Online:2015-12-03 Published:2015-04-25
  • Contact: 华能集团科技支撑资助项目(HNKJ13-H06)

Abstract: Taking the modification of ammonia injection grid(AIG) in a coal-fired power plant for instance, the effects of the modification are evaluated through numerical simulation and calculation. The results demonstrate that the two-way regulating function is beneficial to the even distribution of ammonia and it improves the adaptability to the uneven flue gas velocities. Moreover, the relative standard deviation of the outlet NOx distribution declines from 40% to lower than 15%. The modification improves SCR ammonia spraying effectiveness, increases the catalyst life span, eliminates the local high concentration of ammonia slip at the reactor outlet, reduces the risk of downstream ABS corrosion in the air pre-heater, and it therefore helps the coal-fired power plant achieve super-low NOx emissions.

Key words: coal-fired power plant, flue gas denitrification, selective catalytic reduction(SCR), ammonia injection system, modification, numerical simulation

CLC Number: