Electric Power ›› 2013, Vol. 46 ›› Issue (3): 73-77.DOI: 10.11930/j.issn.1004-9649.2013.3.73.4

• Generation Technology • Previous Articles     Next Articles

Analysis on Condensate Return Water Temperature Anomaly in ACC Systems for600-MW Thermal Units

ZHAO Shuang1, LI Xi-jun2, PING Shi-bin2   

  1. 1. Inner Mongolia University of Technology, Huhhot 010051, China;
    2. Inner Mongolia Daihai Electric Power Generation Co. Ltd., Ulanqab 013700, China
  • Received:2012-10-27 Online:2013-03-05 Published:2015-12-10

Abstract: It has taken place several times at a power plant that the condensate return water temperature and the vacuum temperature of the sixth, seventh and eighth streets of theair-cooling condenser are much lower than that of other streets, accompanying water lever waving in the exhaust steam device. The flow condition of the condensate in ACC is analyzed with the exclusive method, which concludes that there is air leakage on the B side of the main condensate return water pipe of the three streets. Therefore, some measures against the leakage are put forward to address these issues.

Key words: direct air-cooled system, condensate return water, temperature anomaly, water level fluctuation

CLC Number: