中国电力 ›› 2013, Vol. 46 ›› Issue (12): 113-117.DOI: 10.11930/j.issn.1004-9649.2013.12.113.4

• 节能与环保 • 上一篇    下一篇

600 MW超临界发电机组污染物脱除及排放

王运军1, 王宏伟1, 魏继平1, 高建康1, 郭晓民2   

  1. 1. 山西省电力勘测设计院,山西 太原 030001; 2. 霍州发电厂,山西 霍州 031514
  • 收稿日期:2013-09-18 出版日期:2013-12-23 发布日期:2015-12-10
  • 作者简介:王运军(1980—),男,山西山阴人,工学博士,工程师,从事电站设计、洁净煤发电与燃煤污染物控制技术研究。
  • 基金资助:
    国家工程资助项目(发改委发改办能源[2007]2469号)

Removal and Emission of Pollutants from 600-MW Supercritical Units

WANG Yun-jun1, WANG Hong-wei1, WEI Ji-ping1, GAO Jian-kang1, GUO Xiao-min2   

  1. 1. Shanxi Electric Power Exploration & Design Institute, Taiyuan 030001, China; 2. Guodian Huozhou Power Plant, Huozhou 031514, China
  • Received:2013-09-18 Online:2013-12-23 Published:2015-12-10

摘要: 在关停并拆除的老小机组的场地上建设大容量、高参数的新机组,进行“上大压小”技术改造,是电力企业转型、设备更新换代的必经之路。配套建设的高效电除尘器、脱硫、脱硝等烟气净化设施,可使新机组的污染物排放率大幅下降。以国电霍州发电厂“上大压小”改扩建工程1号机组为例,介绍新安装600 MW超临界发电机组SCR脱硝装置、五电场静电除尘装置和石灰石-石膏湿法脱硫装置对燃煤电站煤粉燃烧过程中产生的NOx、烟尘和SO2的脱除效果。现场测试结果表明,在满负荷运行工况条件下,A、B两侧SCR脱硝反应器对NOx的脱除效率为70%~80%,五电场静电除尘器对烟尘的脱除效率为99.85%,湿法脱硫装置对SO2的脱除效率在98%以上,所排放的NOx、烟尘和SO2满足现行火电厂大气污染物排放标准。改造后的2×600 MW机组与改造前的4×100 MW机组相比,污染物排放总量大幅下降,“上大压小”技术改造真正起到了增产减污的作用。

关键词: 600 MW燃煤机组, SCR脱硝装置, 静电除尘, 湿法脱硫, 污染物排放

Abstract: During the transformation of power generation enterprise and corresponding equipment upgrade, it is inevitable to build large- capacity and high-parameter units on the original site with old small units which were shut down and demolished due to the requirements of this technical reform. The construction of a complete set of high-efficiency electrostatic precipitators and gas purification facilities such as desulfurization and denitrification facilities can significantly reduce the pollutant emissions. Taking the Unit 1 in the transformation and expansion project of Huozhou Coal-Fired Power Plant for instance, the paper introduces the effects of the SCR denitrification equipment, five-field electrostatic precipitator and wet flue gas desulphurization(WFGD) equipment on the removal of NOx, dust and SO2 produced during coal combustion. Field tests show that under the full load condition, the NOx removal efficiency by the A and B sides of SCR is in the range from 70% to 80%, while the dust removal efficiency by the electrostatic precipitator is around 99.85%, and the SO2 removal efficiency by the WFGD equipment is over 98%, which meet all the present standards related to pollutant emissions from coal-fired power plants. Moreover, in comparison with the demolished four 100-MW units, the total emissions from the two newly built 600-MW units have decreased significantly, which proves that the substitution of small units with large ones can definitely attain the goal of generation increase and emission reduction.

Key words: 600-MW coal-fired unit, SCR denitrification equipment, electrostatic precipitator(ESP), wet flue gas desulphurization (WFGD), pollutant emission

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