中国电力 ›› 2014, Vol. 47 ›› Issue (9): 18-24.DOI: 10.11930/j.issn.1004-9649.2014.9.18.6

• 电厂自动化专栏 • 上一篇    下一篇

采用机炉电联合控制解决输电线路容量限制引起的机组限出力问题

杨震力   

  1. 神华国华(舟山)发电有限责任公司,浙江 舟山 316012
  • 收稿日期:2014-05-06 出版日期:2014-09-18 发布日期:2015-12-10
  • 作者简介:杨震力(1968—),男,浙江温州人,高级工程师,从事火电厂运行机组热工自动化系统维护检修、基建机组安装调试管理、技术监督及专业技术管理工作。E-mail: 13587068981@163.com

Solutions to Generation Output Constrained by Power Line Transmission Capabilities

YANG Zhen-li   

  1. Zhejiang Shenhua Guohua Zhoushan Power Generation Co., Ltd., Zhoushan 316012, China
  • Received:2014-05-06 Online:2014-09-18 Published:2015-12-10

摘要: 某发电厂3号300 MW燃煤发电机组由于输电网结构的改变,受《电力系统安全稳定导则》的N-1原则的限制,机组从原能满负荷运行的状态,变为只能限出力在215 MW以下运行。为了释放机组出力,通过技术研究,采用机、电、炉联合控制方式,解决了机组限出力的困局。研究内容分为线路过负荷电气判断和热机快速减负荷控制,电气过载信号的触发采用硬件的配置与逻辑的优化2个方面实现,并设有当快速减负荷失败时由电气动态监测控制装置发出跳机指令。研究结果已正式投入工程应用,提高了输电线路输送容量利用率。

关键词: 输电线路, 机组出力, 负荷控制, 过负荷, DEH阀门, PCV阀门, 快减负荷

Abstract: Due to the change of the power transmission network infrastructure, to be compliant with the N-1 principle in“Power System Security and Stability Guideline”, the Unit 3 in Zhoushan Power Plant has to reduce its MW generation from the original full load down to only 215 MW. In order to maximize the output power, a joint control mode integrated with the steam turbine, boiler and outgoing line together is adopted, which solves the dilemma of unit MW output limitation. In this paper, the study on the line overload determination via electrical signals and also the fast load-shedding control are introduced. The electrical overload signal is triggered by hardware configuration and logic optimization. Instructions are issued to trip the unit from the electrical dynamic monitoring control equipment when fast load-shedding scheme fails. The engineering application is put into practice, which shows great improvement of the utilization rate of the transmission line capacities.

Key words: transmission line, output power, load control, line overload, DEH valve, PCV valve, fast load-shedding

中图分类号: