中国电力 ›› 2013, Vol. 46 ›› Issue (3): 68-72.DOI: 10.11930/j.issn.1004-9649.2013.3.68.4

• 发电 • 上一篇    下一篇

1 000 MW火电机组协调控制策略优化

钱朝明, 王会, 吴永存, 罗志浩   

  1. 浙江国华浙能发电有限公司,浙江 宁波 315612
  • 收稿日期:2012-11-28 出版日期:2013-03-05 发布日期:2015-12-10
  • 作者简介:钱朝明(1975—),男,安徽铜陵人,工程师,从事热工自动控制研究。E-mail: qiancm_007@163.com

Optimization of Coordinated Control Strategy for 1 000-MW Thermal Power Units

QIAN Chao-ming, WANG Hui, WU Yong-cun, LUO Zhi-hao   

  1. Zhejiang Guohua Power Company Limited, Ningbo 315612, China
  • Received:2012-11-28 Online:2013-03-05 Published:2015-12-10

摘要: 介绍了1 000 MW超超临界直流炉的控制特点,分析了某电厂1 000 MW火电机组投产后协调控制系统存在的问题,针对变负荷工况下机组主蒸汽压力经常超压、欠压以及锅炉管壁超温的问题提出了控制系统优化策略,从锅炉主控回路、给水控制回路、燃料控制回路等方面进行了控制策略优化和控制参数优化;对锅炉滑压曲线进行了经济优化,最大限度地减少主汽门节流损失,以提高机组经济性,并对实施效果进行了分析和总结。

关键词: 1 000 MW火电机组, 协调控制, 策略优化

Abstract: Based on the introduction to the characteristics of the control over 1 000-MW ultra-supercritical once-through boilers, the problems of the coordinated control system existing in the 1 000-MW unit in on power plant are analyzed. The control system optimization strategies on main steam over/under pressure and tube wall overheating in load variation are put forward. In addition, the optimized control strategies and parameters for main control circuit, feedwater loop and fuel loop are proposed. Meanwhile, the boiler sliding pressure curve is optimized to minimize the throttling losses of the main steam valve and improve the economic performance of the unit. Finally, the effects of the implementation of these strategies are analyzed and summarized.

Key words: 1 000-MW thermal power unit, coordinated control, strategy optimization

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