中国电力 ›› 2017, Vol. 50 ›› Issue (11): 180-184.DOI: 10.11930/j.issn.1004-9649.201707045

• 节能与环保 • 上一篇    

炉水磷酸盐多参数协同自动加药控制系统的构置与应用

任治民1, 朱志平2, 金绪良3, 李永立4, 王应高4, 赵强1, 乔越2   

  1. 1. 内蒙古岱海发电有限责任公司,内蒙古 凉城 013700;
    2. 长沙理工大学,湖南 长沙 410072;
    3. 中国大唐集团科学技术研究院有限公司,北京 100043;
    4. 华北电力研究院,北京 100045
  • 收稿日期:2016-09-01 出版日期:2017-11-25 发布日期:2017-11-29
  • 作者简介:任治民(1966—),男,甘肃平凉人,硕士,高级工程师,从事电厂管理工作。E-mail: renzhm@daihaipower.com

Configuration and Application of Coordinated Multi-Parameter Automatic Control System for Boiler Water Phosphate Dosing

REN Zhimin1, ZHU Zhiping2, JIN Xuliang3, LI Yongli4, WANG Yinggao4, ZHAO Qiang1, QIAO Yue2   

  1. 1. Inner Mongolia Daihai Power Generation Co., Ltd., Liangcheng 013700, China;
    2. Changsha University of Science and Technology,Changsha 410114, China;
    3. China Datang Corporation Science and Technology Research Institute Co., Ltd., Beijing 100043, China;
    4. North China Electric Power Research Institute Co., Ltd., Beijing 100045, China
  • Received:2016-09-01 Online:2017-11-25 Published:2017-11-29

摘要: 随着火电厂对汽水品质要求的不断提高,人工调节加药的方式逐渐被自动加药所替代。目前自动加药系统多采用基于单一参数的PID控制,受限于炉水磷酸根监测、加药控制的时滞性,在机组调峰及变负荷运行时不能对磷酸根浓度进行精确调节。针对这一缺陷,提出了炉水磷酸盐多参数协同加药控制方案,其要点是引入炉水的磷酸根含量、pH值、电导率和给水流量4个控制参数,并将炉水pH值、炉水电导率值计算结果与在线监测的炉水磷酸根浓度相互校正,同时结合锅炉给水流量变化情况,采用智能PID控制技术调整磷酸盐加药量。内蒙古某电厂采用该方案对原加药系统进行了改造,实践结果表明,炉水磷酸盐多参数协同自动加药控制系统运行后,炉水磷酸根含量得到稳定控制,pH值为9.40~9.50,电导率为9.5~10.5 μS/cm,炉水水质合格率大大提高,为机组安全稳定运行提供了保障。

关键词: 火电厂, 炉水处理, 炉水pH值, 自动加药, 多参数控制, 智能PID控制

Abstract: With the ever-increasing requirements for steam and water quality in thermal power plants, manual dosing has been gradually replaced by automatic dosing. Currently in most automatic dosing systems single-parameter based simple PID control is utilized. However, limited by phosphate monitoring and control delay, this type of control cannot accomplish accurate and immediate regulation of phosphate concentration under peak modulation or variable load conditions. Regarding these problems, this paper proposes a multi-parameter automatic control system for boiler water phosphate dosing. The program introduces the phosphate concentration, pH value, and conductivity of boiler water together with the boiler feedwater flow as the control parameters. The calculation results of pH value and conductivity value of boiler water are corrected with the on-line monitored phosphate concentration. At the same time, in combination with the boiler feedwater flow changes, the intelligent PID control technique is used to adjust the dosage of phosphate. The program has been implemented in the dosing system innovation project in an Inner Mongolia power plant. The results show that since the commissioning of the multi-parameter automatic control system into operation, the phosphate content has been stabilized with the pH value maintained between 9.40 and 9.50 while the conductivity between 9.5 and 10.5 μS/cm in boiler water. Apparently, the boiler water quality is greatly improved, which ensures the safe and stable operation of the generation unit.

Key words: thermal power plant, boiler water treatment, pH value of boiler water, automatic dosing, multi-parameter control, intelligent PID control

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