中国电力 ›› 2014, Vol. 47 ›› Issue (11): 26-29.DOI: 10.11930/j.issn.1004-9649.2014.11.26.3

• 发电 • 上一篇    下一篇

300 MW机组过热器喷水减温控制研究与改进

郑伟1, 2, 赵猛3   

  1. 1. 天津职业大学机电工程与自动化学院,天津 300410;
    2. 天津大学电气与自动化工程学院,天津 300072;
    3. 天津华能杨柳青热电有限责任公司,天津 300380
  • 收稿日期:2014-07-09 出版日期:2014-11-18 发布日期:2015-12-08
  • 作者简介:郑伟(1983—),男,天津人,博士研究生,工程师,研究方向为自动化控制和智能系统。E-mail: da_zhengwei@126.com

Research and Improvement of Superheater Spray Desuperheating Control in 300-MW Units

ZHENG Wei1, 2, ZHAO Meng3   

  1. 1. School of Mechatronical Engineering and Automation, Tianjin Vocational Institute, Tianjin 300410, China;
    2. School of Electrical Engineering and Automation, Tianjin University, Tianjin 300072, China;
    3. Tianjin Huaneng Yangliuqing Thermo Power Co., Ltd., Tianjin 300380, China
  • Received:2014-07-09 Online:2014-11-18 Published:2015-12-08

摘要: 某电站300 MW机组在过热器主蒸汽温度喷水减温控制中,存在喷水不均匀、现场设备故障频发和面对扰动温度失调等现象,严重影响了机组运行的可靠性和经济性。为了改善对过热器主蒸汽温度的控制调节,通过应用温差控制和自适应控制,增加抗积分饱和功能和微分前馈逻辑,以及改进现场设备等方法,使喷水减温控制取得了良好的效果。机组实际运行结果表明,优化改进达到了预期目的,从而保证了机组运行的安全高效。

关键词: 火电机组, 主蒸汽温度, 喷水减温, 自适应控制, 温差控制, 微分前馈

Abstract: During the spray desuperheating control of the main steam temperature of a 300-MW unit, uneven spraying, frequent equipment faults and control failure on temperature disturbance exist, which severely affects the reliability and economy of the unit operation. In order to improve the control level of the main steam temperature, the temperature difference control and the self-adaptation control are applied, integral saturation resistance function and derivative feedforward logic are enhanced and the field equipment is improved. The adoption of these methods results in better spray desuperheating control. The unit operation indicates that the optimization and improvement have reached the expected goal and made the whole unit safer and more efficient.

Key words: thermal generating unit, main steam temperature, spray desuperheating, self-adaptation control, temperature difference control, derivative feedforward

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