中国电力 ›› 2017, Vol. 50 ›› Issue (1): 181-184.DOI: 10.11930/j.issn.1004-9649.2017.01.181.04

• 节能与环保 • 上一篇    

锅炉脱硝装置运行对高背压供热机组影响分析

徐君诏   

  1. 华能新疆能源开发有限公司,新疆 乌鲁木齐 830017
  • 收稿日期:2016-09-03 出版日期:2017-01-20 发布日期:2017-01-23
  • 作者简介:徐君诏(1980-),男,河北沧州人,工程师,从事电力生产技术与节能管理工作。E-mail: junzhao_xu@163.com

Impact Analysis of Boiler De-NOx System on High Back Pressure Heat Supply Units

XU Junzhao   

  1. Huaneng Xinjiang Energy Development Co., Ltd., Urumqi 830017, China
  • Received:2016-09-03 Online:2017-01-20 Published:2017-01-23

摘要: 近些年由于环境污染问题日趋严峻,城市周边的供热机组锅炉都安装了烟气脱硝装置,而烟气脱硝装置的运行对高背压供热系统有一定的影响。通过对高背压供热系统热力特性分析,得出锅炉最低脱硝负荷是制约高背压供热系统经济运行的主要因素,提出高背压供热机组实现脱硝装置全负荷运行改造方案,以某电厂135 MW高背压供热机组分析,实施改造后将降低供电煤耗8.67 g/(kW·h),进一步挖掘了高背压供热机组的节能降耗潜力。

关键词: 火力发电机组, 高背压供热机组, 烟气脱硝装置, 经济性

Abstract: In recent years, all boilers for civic heat supply units have been equipped with flue gas denitrification device due to the increasingly severe consequences of environmental pollutions. However, the operation of the flue gas denitrification device has exhibited some side effects on the high pressure heat supply system. In this paper, through the analysis on the thermodynamic properties of the heat supply system, it is concluded that the boiler minimum denitrification load is the major factor restricting the high pressure heating system economic operation. As a result the retrofit plan is proposed to fully take advantage of denitrification device for high back pressure heating unit under all loading conditions of. The case analysis of a 135-MW such unit indicates that the net coal consumption rate will be reduced by 8.67 g/(kW·h) once the plan is implemented. In this way the potential of energy saving in high back pressure steam turbines can be further explored.

Key words: thermal generation unit, high back pressure heating unit, denitrification device, economic performance

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