中国电力 ›› 2015, Vol. 48 ›› Issue (9): 157-160.DOI: 10.11930.2015.9.157

• 节能与环保 • 上一篇    

石灰石-石膏湿法烟气脱硫系统浆液起泡原因分析

贾西部,金万元,李兴华,赵彩虹   

  1. 1. 西安热工研究院有限公司,陕西 西安 710032;
    2. 内蒙古岱海发电有限责任公司,内蒙古 凉城 013700
  • 收稿日期:2015-05-04 出版日期:2015-09-25 发布日期:2015-11-25
  • 作者简介:贾西部(1982—),男,陕西渭南人,从事烟气脱硫系统烟气净化、性能检测、化学分析等。E-mail: JXB_fengqiang1018@163.com

Cause Analysis on Slurry Foaming in Wet Limestone-Gypsum Flue Gas Desulfurization System

JIA Xibu, JIN Wanyuan, LI Xinghua, ZHAO Caihong   

  1. 1. Xi’an Thermal Power Research Institute Co., Ltd., Xi’an 710032, China;2. Inner Mongolia Daihai Electric Power Generation Co., Ltd., Liangcheng 013700, China
  • Received:2015-05-04 Online:2015-09-25 Published:2015-11-25

摘要: 石灰石-石膏湿法脱硫吸收塔浆液因起泡而溢流的现象时有发生,影响脱硫系统安全运行。为探究吸收塔浆液起泡原因,从浆液起泡机理入手,对若干电厂脱硫系统浆液和泡沫样品进行了成分及电镜分析。研究结果表明:脱硫系统工艺水水质、烟气粉尘含量及石灰石品质均对脱硫吸收塔浆液起泡有促进作用,但各电厂侧重不同。首先,应避免将吸收塔中的溢流物质返回吸收塔本体,再根据各电厂不同情况采取相应措施,即可避免出现吸收塔泡沫溢流问题,或使该问题得以缓解。

关键词: 石灰石-石膏湿法脱硫, 浆液起泡, 表面张力, 粘度

Abstract: Slurry overflow happens from time to time due to slurry foaming in the absorber of the limestone-gypsum wet desulfurization system, which may endanger the operation of the flue gas desulfurization system (FGD). To find out the foaming causes, the composition and electrical microscope analysis on some FGD slurry and foaming samples is conducted from the aspect of foaming mechanism for different power plants. The results show that the FGD flue gas dust concentration, limestone and process water qualities all will promote slurry foaming, but the severity effects may vary in different plants. To eliminate or alleviate the foaming overflow problem, power plants should first prevent the overflowing liquid from going back to the absorber and then take corresponding measures according to their own situation.

Key words: FGD, slurry foaming, surface tension, viscosity

中图分类号: